Development of a Low Speed Wind Tunnel Test Campaign

Detta är en Master-uppsats från KTH/Flygdynamik

Sammanfattning: This study was performed to investigate aerodynamic characteristics of the 37.5% scaled­ down Green Raven MK18 airframe, to evaluate boundary corrections method, and to investigate on support interference. A wind tunnel test was originally planned on June 2021 at a Large­Low­Speed Wind Tunnel at University of Bristol; however, due to COVID­19 travel restrictions, the test has been postponed to November 2021. In or­der to supplement the work and data directly required for the test, computational fluid dynamics (CFD) investigations were performed in free air and in wind tunnel condi­tions, both with and without support interference, at a Reynolds number of 7E+05. The simulations utilized an incompressible Reynolds-­Averaged­-Navier.­Stokes equa­tion accompanied with k − ω SST for turbulent modelling. Corrections factors were obtained to compensate for wall interference, and results indicate a satisfactory agree­ment between free ­air and wind­ tunnel corrected data for wall interference. The sup­ port structure interferes with the aerodynamic loads produced by the model. Lift and drag decrease, and pitching moment increases compared to WT without support structure condition.

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